Critical crack path assessments in failure investigations
This paper presents a case study in which identification of the controlling crack path was critical to identifying the root cause of the failure. The case involves the rupture of a 30-inch (0.76 m) natural gas pipeline in 2010 that tragically led to the destruction of a number of homes and the los...
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Main Author: | |
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Format: | Article |
Language: | English |
Published: |
Gruppo Italiano Frattura
2015-10-01
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Series: | Fracture and Structural Integrity |
Subjects: | |
Online Access: | http://www.gruppofrattura.it/pdf/rivista/numero34/numero_34_art_13.pdf |
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Summary: | This paper presents a case study in which identification of the controlling crack path was critical to
identifying the root cause of the failure. The case involves the rupture of a 30-inch (0.76 m) natural gas pipeline
in 2010 that tragically led to the destruction of a number of homes and the loss of life. The segment of the
pipeline that ruptured was installed in 1956. The longitudinal seam of the segment that ruptured was supposed
to have been fabricated by double submerged arc welding. Unfortunately, portions of the segment only
received a single submerged arc weld on the outside, leaving unwelded areas on the inside diameter. Post-failure
examination of the segment revealed that the rupture originated at one of these unwelded areas. Examination
also revealed three additional crack paths or zones emanating from the unwelded area: a zone of ductile tearing,
a zone of fatigue, and a zone of cleavage fracture, in that sequence. Initial investigators ignored the ductile tear,
assumed the critical crack path was the fatigue component, and (incorrectly) concluded that the root cause of
the incident was the failure of the operator to hydrotest the segment after it was installed in 1956. However, as
discussed in this paper, the critical path or mechanism was the ductile tear. Furthermore, it was determined that
the ductile tear was created during the hydrotest at installation by a mechanism known as pressure reversal.
Thus the correct root cause of the rupture was the hydrotest the operator subjected the segment to at
installation, helping to increase the awareness of operators and regulators about the potential problems
associated with hydrotesting. |
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ISSN: | 1971-8993 1971-8993 |